January - December 2016
The original Blue Bess 360 has had an oil change and a change
of leads. So it all looks ready to go although a quick check did
inevitably show that there was another problem - a leak from the
exhaust gasket where the front downpipe joins the manifold.
Hence a couple of trips to the car are spent dismantling the
front exhaust by removing the bolts at the offending junction,
removing the manifold bolts and the various bolts that hold the
front downpipe onto the bell-housing and the racket on the
rear-side of the engine. Finally it all comes apart and a trip
to the nearest motor spares shop allowed a new exhaust gasket to
be procured. Indeed the shopkeeper said 'Pay next time you're in
the shop' which is even more awesome than usual. The gasket will
soon be fitted.
A bit of time has been spent cleaning-up all the mating faces
and 'copper-easing' the threads everywhere so it will hopefully
go back together a bit more easily than it otherwise
would.
Mid-January 2016 has seen the exhaust manifold refitted with a
fairly generous dose of exhaust pipe putty at the junction, amid
great arguments among neighbouring garage tenants over parking
and other such tifles. A quick test shows that the seal seems to
be holding and a drive-around shows that everything else to do
with the car seems to be pretty-much OK, so it may be time to
put this one back into action as the main form of transport for
the foreseable future to give the dark blue 1.7 a bit of a rest
in the worst of the winter.
Mid-Feb 2016 and the 360 develops an annoying screech which I
initially attribute to loose belts on the power-steering pump and
the alternator. However, various checks on the belts and efforts
to stop them squealing with a spray-on sticky type of substance do
not make any difference. I then notice that the headlights are
getting dim to the point where I can hardly see where I am driving
at night and the rear windscreen wiper is painfully slow, not to
mention that fact that the battery seems to die after every trip.
It is all pointing to a failure of the alternator brushes so the
car is returned to storage again whilst I wait for a refurbished
alternator to arrive in the post. Meanwhile the 1.7 is given a
hasty clean-out, wash and polish and is pressed back into everyday
use and it seems to be a better car all-round really. The 360 has
had various half-hearted efforts to stop the exhaust banging, etc,
which have almost worked, but its not as well hung-together as the
newer 1.7, although the latter is a damned-sight colder since I
still haven't replaced the thermostat (shame, but many efforts to
keep another of my wrecks on the road have taken up too much
time). So lets 1.7 it up for now while the 360 gets a bit of
electro-mechanical attention.
The old alternator on the 360 is removed and replaced anew which
cures the poor charging and screeching problems that I reported
above.
The 360 is returned to everyday use and gets to go on quite a long
run in late Feb 16. Fully independent and verifiable confirmation
of this can be found in the following photos, kindly taken by
Reading Council, which show her passing underneath the arches of
the Great Western Railway, while completely lost and giving a lift
to someone. OK, I didn't expect the fast lane to be for buses
only, but the fine isn't as bad as the last one and, fortunately,
they didn't catch me making an even bigger mistake later on - I
was tipped-off by someone who kindly waved frantically at me, just
in time.
However, now in early-mid March 2016, the car does not sound like
it is idling very smoothly and a few tweaks to the mixture give
only a temporary cure to the poor idle. I take the car to the
garage for a bit of wheel-balancing and tracking and I mention the
poor idle. They say they will give it a tune but a day or so later
I find out that it is refusing to start at all in their hands due
to no spark and, having replaced the flywheel sensor, they think
it is the electronic ignition unit. Hence a couple of spare
Renix's and a new coil are found in the roof and taken to the
garage for them to play with. A day or so later, still no spark at
all with any of the renixes so I suggest that it may be the
connections on the back of the fuse box, but they do not believe
me - its such a hard life. I think the fuse box connections have
gone wobbly when they jacked the car up. How's that for a theory?
So the current plan is to retrieve the car and have a fiddle with
it myself. Should be fun - indeed they seem keen to get rid of it,
too!!
The car is recovered by the garage blokey towing it with me at the
steering wheel and on making a right-turn, the tow-bar folds on
itself and quite badly clonks the front valance - which is not
fun. Thus trying to rescue this car from the clutches of those
who, whilst being very well-meaning, probably don't have the time
to give this old banger all the care it deserves, the poor beastie
is damaged (thankfully only slightly). Anyhow this should be a
bang-out-able dent so I am hoping that with the benefits of more
time on my side, the better weather and the driving force of guilt
and despair, I will get a move-on with sorting it out and will
probably be canonised in the process. Amen.
A weekend is spent un-doing what the garage have done. I
cleaned-up the connections at the back and front of the fuse-box -
they were all pretty good, but an extra clean-up should do no
harm, although in the end, it actually made no difference at all
to the ignition trouble. I then fitted the original renix unit
with the new coil which the garage had used which again made no
difference. I then found that the problem definitely lay in the
new flywheel sensor which the garage had fitted - it simply didn't
work and the car's ability to make sparks could be regenerated by
cleaning-up and re-fitting the old flywheel sensor. Its a bit
stally so there may still be some weakness in the spark or some
carburretor gasket leaks, but its better than not working at all.
Anyhow, since most of the work involves lying in the driver's
footwell in the dark, the photos aren't so good, but I did manage
to get a decent one of the fuse box connections (above) which
shows the hole that always goes dodgy. Its in the brown connector
on the right-hand side of the hole in the bulkhead, right-hand
column of holes, middle hole. So the plan is now the repair the
front valance, which will involve finding a reasonably large
hammer.
Firmly in the middle of March 2016 and the photos below clearly
show the dent in the front valance caused by the dodgy old
tow-bar. The good news is that some progress has been made in
hammering it out by removing the front bumper (again) and use of a
wooden dolly with a fairly large hammer. The final stages will
need a G-clamp, or two, to bend back some of the stretched metal
at the edge of the valance, although none of this is too bad
really. I could just paint it all over with underseal but the
perfectionist in me says I have to try to straighten the metal
first. A crowbar might also help to push the top flat part down a
bit so mental note to self to remember to take that crowbar is
made.
Its now the end of March 2016 and the work to complete the repairs
to the front valance has been, err, completed, as I hope the
photos show. First of all, here's how it looked after a bit of
hammering-out from the inside with a custom-made wooden dolly.
Well, not too great, but its OK.
So now its time for a paint-up with underseal to try to make-up
for the shortfall in the shortfall in the metal-strightening
efforts. This is followed by some painting with grey-primer.
Its not looking too bad, so a bit of blue paint by Halfords
aerosol, brush and finally aerosol, again, brings it back to
almost the right colour (Volvo paint code 219-5). Some waxoyling
around the underside for good measure adds a bit of confidence,
too.
Combine all of this with a mega-triumph in discovering that the
carburettor gaskets were in a completely wrecked state, a bit of
home-made gasket-making sees everything going pretty-much in the
right direction in terms of repair and reassembly. Indeed the
carby gasket leaks must have been the root-cause of the
poor-idling which caused all of this trouble in the first place.
With perfect timing, the dark blue 1.7 suffers an exhaust
centre-section failure, so the, now almost fully-repaired,
metallic blue 360 is itself given a new rear exhaust hanger and
then pressed back into everyday action. It now idles happily at
500 rpm and does not stall at all on pulling-away. Epic inebriated
awesomeness abounds and emanates everywhere. Meanwhile, amongst
all of this chaos, the red 1.7 3-door still starts and runs fine
after some 3 months of waiting patiently for me to begin some
cosmetic improvements - still on the cards, but they will happen.
Ok, so I've been a bit slow to keep this up-to-date, again, but
April 2016 has seen the middle section of the dark blue 340's
exhaust replaced and seemingly the job has been successful - or at
least the car does not make that deafening noise any more!
Things are starting to move on the Red Ness front with the engine
starting and running extremely well after a long rest and some
wire brush work has been done to the underside in readiness for a
coat or two of waxoyl.
As can be seen, there is some surface rust but its not too bad at
all, really. I think the brake line across the back axle will need
renewing with a bit of copper pipe and the handbrake mechanism
will probably need freeing-up where it passes through the backing
plate and inside the drum.
Anyhow, at the end of April 2016, the waxoyling is starting to
make some progress.
Early May 2016 has seen the rear end of the red one raised up on
axle stands for some more waxoyling and the rear wheels removed
for tackling the brake drums which seem a bit sticky. The drums
appear to have had a fairly hard life in the rust-friendly
environs of Shropshire.
Anyhow, the drum on one side came-off alright in the end after
loosening the hand-brake cable and some tapping and prising work
on the drum itself. The inside looks pretty good and will be
cleaned-up and dismantled to check the lever device that goes
through the backplate which is awesomely good at getting seized-up
with rust. The drum will need a rotary wire-brush with a drill and
a bit of grinding to remove the lip which develops on the inside
due to wear caused by the brake shoes. The shock absorbers will
need replacing due to the outer sleeves rusting through but
everything else seems to be pretty good. I think the brake pipes
can be rescued with a bit of paint to keep the surface rust at
bay.
A few days later the paraphernalia within each of the brake drums
is inspected and it is found that the seals on the cylinders are
leaking quite a lot now that they don't have so much pressure on
them. The little circular springs also seem to be missing. Anyhow
its looking like new brake cylinders, or at least new seals, are
on the cards.
The shoes and springs are removed and stored for safe-keeping and,
hopefully, ease of reassembly!!
The pipes on the back of each brake cylinder refuse to unbolt so
the pipes, sadly, have to be cut through with a hacksaw, but they
will all be replaced anew. The cylinders themselves unbolt
relatively easily and this allows removal of the self-adjuster
lever mechanism which was seized at both ends, on both sides of
the car.
A bit of wire brush work on the drum back plates will allow them
to be painted with a bit of Kurust so perhaps we are beginning to
make some progress.
During May 2016, some work is done to paint the inside of the rear
brake back-plates with Kurust, to reasonably good effect, I hope.
Some more waxoyling is done on the back-axle and the drums
themselves are rubbed-down, their ridges ground-off and their
outsides given a dose of Kurust. Slowly, new copper pipes and
brake cylinders are fitted in place on the back axle.
After much struggling, the brake shoes and springs are refitted on
one side with a smear of copper-ease for lubrication on the
backplate where the sides of the shoes rub. Its all going a bit
more slowly than I had hoped, but some time is being spent on
another of my ruins ;-0
Finally, after a monu-mental struggle to get the final brake-shoe
retaining spring into place, the job is done on the other side of
the car, too, and the Kurusted drums are replaced, the brake pipes
tightened-up and the wheel arches given a light wire-brushing in
preparation for some more waxoyl.
Now in early June 2016 and Red Ness has had some of the dried mud
under her rear wheel arches wire-brushed away in readiness for
some waxoyl.
So far, two coats of waxoyl have been applied to reasonably good
effect and the old shock-absorbers have been removed.
New shock absorbers are fitted and everything looks awesome again.
Following these successes things take a slight turn for the worse
since efforts to check the differential oil level by removing the
filler plug result in the diff-backplate tearing, as (just about)
shown below. Ok, it was tight so I had to use the jack to try to
undo it, but it wasn't budging. Hence the backplate will have to
be removed and probably will be taken to the welder for repair,
but this will have to be done on a slightly slower timescale since
other tasks leer their ugly heads.
One such task is created by my eventual loss of patience with the
banging exhaust pipe on the 360. I had previously got my annoyance
to manageable levels by fitting two ultra-strong polyurethane
hangers from Classic Swede and these worked well at stopping the
knock. However, wherever there is competence, there is ambition,
and these two excellent bushes made a bid for freedom and were
never found again, despite my walking about two miles along the
offending country lane where they escaped. Anyhow, I replaced
these with two strong rubber ones which also worked well in cold
weather, but now the warmer weather is with us, they became
considerably more flexible and therefore do not prevent the
exhaust pipe banging any more. To save my sanity, everyday
transport is shifted temporarily to the beautiful blue 1.7 and off
comes the 360's rear silencer for attention. Indeed, fully
independent and verifiable proof of my transition to driving the
1.7 is kindly provided by Kingston Council following my errant
excursion into one of their lovely yellow boxes and yet another
fine ensues, bah humbug.
Meanwhile, some smithy work with a blow-lamp and a heavy hammer
eventually got the 360 exhaust pipe beaten into a state where,
finally, on re-fitting it to the car, I find that it does not bang
anymore when going over bumps and dips in the road. That really is
an outstanding breakthrough of inestimable proportions and allows
me to return to working on the underside of the red 1.7.
A wire brush and a bit of paint has also been applied to both of
Red Ness's rear wheels while I waited to get started on the
diff-backplate, a glance at which shows some prominent rust.
After several visits and much brain-aching about which trick to
try next, the backplate is finally removed in late June 2016.
On removing the diff cover plate, it is pretty clear that it is
quite badly rusted and I have a memory of a spare being somewhere
in the roof and this is duly found. The two side by side now show
that it is definitely going to be better to replace the old one so
a new gasket is ordered.
Now getting towards the last week of July 2016 and there hasn't
been much time that I can spent on the 340 due to self-inflicted
pressure to sort out my other ruin, but the 360 is used as daily
transport for ferrying bits of woodwork in various states of
repair for said ruin, as the photos below will show. Shame that a
welder decided to remove this veneered panel with a crowbar - I
know its beauty is only skin deep, but it only takes about a
couple of hours to remove it non-destructively!
Anyhow, I should be back on track with the 340's in a few weeks.
It is now mid-August 2016 and I am getting progressively closer to
re-starting restoration work on the red beastie. Hopefully this is
evidenced by the arrival of an excellent Mac gasket set for the
differential cover plate and by the application of a coat of
Hammerite black paint to said diff cover whilst closely supervised
by Socks in the cat department. As the instructions say, I must
remember to clean out the breather box.
Indeed, the breather box is checked and found to be clean so the
diff coverplate is given a bit blue sealant around the seams and
the gasket is given a light coat of it, too. The mating-face on
the diff itself is found to be clean (I must have done that
before) as well as being given a bit of sealant and everything is
bolted-up loosely (finger-tight with the allen key) to let the
sealant set a bit before the bolts are tightened to the right
torque and any oil is added. The plan is to leave it for a week or
two to let the sealant set.
Meanwhile, the plan is to get the brakes bled-through so that the
car might eventually be put back on the ground and reversed out of
the garage to allow things to start at the front. However, on
attempting to pressure-bleed the system, I see and hear a fine-jet
of brake fluid escaping from the plastic brake fluid reservoir
that sits on the servo. A closer look shows that someone or
something (maybe even a mouse) has worn away at or chewed through
a little black rubber seal on top of the reservoir and this
therefore looks like another candidate for replacement. That area
of the engine bay is given a copious flush down with water to
minimise the chance of any paintwork being damaged by the brake
fluid and eventually a suitable spare reservoir is found in the
roof. You can just see the offending part which leaked (it looks
like some sort of valve device) right in the middle of the
picture.
The spare reservoir is given a bit of a clean-out, fitted and
re-filled. Thankfully, it seems to work fine since it allows the
rear brakes to be pressure-bled and applying pressure to the pedal
seems to do the right thing. Forever forensic, I make an
'interesting' discovery that the dust-cap on the spare wheel has
been nibbled away in exactly the same manner. There must be a
wild-life expert who can recognise those chew-marks but I am
thinking.... mice.
Anyhow, after a bit less than a week, the bolts on the diff cover
are tightened-up to 22 Nm and then its left to sit for a bit. A
couple of days later they are checked again for tightness and the
diff is refilled with EP80/90 oil. A few days later it looks as
though its not leaking so awesomeness really abounds. As can be
seen, none of this is concours class stuff - its aimed at getting
a working car that is reasonably well rust-protected and the
metalwork tidy, etc.
Consequently, the rear brakes are given another quick pressure
bleed to be sure they are OK, some wire-brushing and waxoyling are
done where needed, the rear-wheels are fitted again and the car is
lowered back onto the ground. Refitting the now charged-up battery
allows the engine to start and run awesomely such that a quick
run-around the garage yard allows the (slightly dusty) car to be
put back into the garage with the front facing out so that work
can commence in this department asap. Meanwhile will contemplate
the rusty front valance and the inner wings which will probably be
left for a few months (to save money ;-) while I tinker with a few
bits and bobs in the engine bay, dashboard, trim, etc.
Now into early Sept 2016 and a few cosmetic-style jobs are done
such as cleaning the dashboard and replacing the radio with a new
one from MAC on the volvo300mania site which has all the knobs
present and correct. It works, too!
By driving the car a bit at the garage, I was reminded that the
switches on the steering column feel a bit loose, so the shroud
beneath the steering wheel is removed and the screws on the
expertly-repaired mounting panel, as well as the ones at the top,
are tightened to brilliant final effect.
I also remember that the car needs some new door seals to cure the
wind-whistle, so a procurement in that department will be looked
at over the next few weeks while I sort out more running issues
with a much worse ruin hidden away elsewhere.
Its now mid-October 2016 and back on the red 340 again with the
purchase of a new 3-door door seal which was fitted, as shown
below, but was found, alas, to make the process of closing the
door almost impossible, even after repositioning both the lock and
catch. Thus it seems that the rubber of the new seal is probably a
bit too stiff and bulbous, so a thinner alternative is sought from
the web.
Meanwhile a bit of an issue with the falling-out-ness of the
interior light switch is resolved with a clipped-off bit of
cable-tie slotted into the right place. This seems to have done
the job OK.
Also, while waiting for the new, new door seal to arrive, the car
is given a bit of a clean and polish to inimitably awesome effect,
in my wholly unbiased view.
Okay, so the thinner door seal arrives and with a bit of a
struggle it can be made to fit pretty well and allows both doors
to close very easily. By testing with an old till-receipt I can
feel that the passenger side door is sealed well all around but
the driver's door seems to have a hairline gap at the top even
after re-adjusting the lock and catch positions. I have a plan
which is to try and ever-so-slightly bend the window frame inwards
using bits of wood, the garage wall and thick blankets to protect
the paint work (with the window wound-down, of course). Whether it
will work, I do not yet know as I currently have no way of seeing
into the future, so this phase is still... a mystery, yet to be
revealed.
A bit of bending about of the driver's door does seem to have
improved the situaish a bit, at least according to the
till-receipt test, so lets hope that, when the car is mobile and
able to go along the bypass, there isn't an excessive
whistle-down-the-wind sound. Indeed, independent verification of
my visits to the car to continue work on it are kindly provided
again by Kingston council, due to my inability to judge how much
space will be left for me when moving forward into that very same
yellow box as before.
And they have even added a bit of Ealing Cinema-style comic film
noir atmosphere to very good effect, too.
Anyhow, we are now at the end of October 2016 and Red Ness has
been raised-up on axle-stands at the front and had her front
wheels removed for some wire-brushing underneath to remove dried
mud and rust. Removing the wheel-nuts was a fairly difficult task,
breaking several tools, but eventually they came undone. The brake
disks seem a bit scored but they may be OK. The biggest thing that
has happened is that brake-disk backing-plate has disintegrated on
the driver's side, but I have at least one satisfactory spare and
maybe a very good one somewhere - but that may be a false memory.
The driver's side calliper is eventually removed as are the pads.
Generally the disks are a bit irregular but not too bad, I hope,
and the pads are a bit seized onto it but I hope they can all be
cleaned-up and copper-eased to good effect without having to renew
anything, apart from that damned backing plate which has
well-and-truly disintegrated in my hands.
A few presses on the brake pedal confirm that the calliper itself
is working fine so if we can remove everything necessary to
replace the backplate, I am hoping that there won't be too much to
do beyond a bit of wire-brushing and painting work. However,
efforts to remove the calliper bracket do not work since the bolts
are well-and-truly rusted in. Even the Irwin kit and the molegrips
will not shift it, so there has to be some other sneaky way to
avoid removing the whole strut.
The backplate itself has now completely crumbled away and a peep
around the back shows some allen bolts holding the disk to the hub
which might be possible to undo, if only I had the right allen
key. Now in early Nov 16, removing the grease cap and the hub-nut
allows the disk-hub assembly to be substantially loosened-up, but
alas not removed fully since the calliper bracket will not let it
go. So a few days later, I return with a bigger set of allen keys
and, after using an 8mm one to undo the bolts holding the disk to
the hub, a bit of hammer-and-chisel work allows me to get it all
apart.
Now all I have to do is remove the (very rusty) little bolts which
hold the remains of the backing plate in place, so copious amounts
of penetrating oil are applied.
Well, in the end it just so happens that three of the bolts came
out fine, but the lowest one at the front snapped-off and this
required a bit of mid-November 2016 drilling work to be done, by
hand for convenience - less hassle than starting my generator and
using the leccy drill instead. Quieter, too.
This allows the remains of the back-plate to be removed by
scraping away at it with a screwdriver, hammer-and-chisel, wire
brush, etc, and this finally reveals the all-important groove
between the calliper mounting bracket and the strut itself which
the backing-plate slots into. This is quite good news because a
trial fit with a spare backing plate suggests its all going to fit
back together OK in the end, hopefully.
Ok, so here we go with a bit of painting Hammerite onto the strut
paraphernalia, but not too thickly because we don't want to block
up that groove.
And here is the new backing plate from the roof (thanks, derskine
;-) which has been given a thin coat of Hammerite, too.
Are you thinking "A lot of photographs for not a lot of work"?
Well you could just be right there, too.
Getting into the second half of Nov 16 and things have been making
progress. The driver's side hub has been muddled back together
over a couple of trips to the car which involved many doings-up of
the allen-key bolts followed by undoing them, to get it all back
together on the stub-axle correctly. There also was a bit of a
B&Q solution to the problem of the bolt which had to be
drilled-out. Well, I'm not going to re-tap the thread am I!!
A fair amount of grease was put inside the hub itself, the outer
bearing replaced, the nut done up to the right torque, then
backed-off 90 degrees and peened over (as per Hades manual) and
the cap filled with grease and tapped into place again.
Then the brake pads and the calliper were replaced after squeezing
the piston in with the special tool and applying a bit of
copper-ease to the places where they rub together and a bit of
thread-lock to the calliper bolts. The rubber gaitor on one of the
calliper bolts in replaced.
A test shows that the setup seems to work OK, releasing the disk
fairly nicely when the brake pedal is released. So now its time to
start the process of bleeding some brake fluid through that side
and this will, of course, involve removing the pesky bleed-nipple
which is well-and-truly rusted-up. So it is given a bit of a
de-rust with a wire brush and screw-driver blade prior to soaking
in copious amounts of penetrating oil for a couple of days.
Well, a couple of days later some cautious efforts were made to
remove the offending nipple with molegrips since the hexagonal
part of its cross-section had rusted away. Anyhow, it was to no
avail since the nipple broke at about half way down. Subsequent
efforts resulted in it breaking further down still which then
allowed use of a screw extractor but this did not work either
since the drill-out part broke-off in the offending nipple. Thus,
efforts are made to remove the whole caliper for sending away to
have the remains of the nipple drilled-out, but on trying to
remove the brake pipe, it all went Pete Tong again since the pipe
itself became coiled-up in an amazing twist and the steel pipe to
which it is fitted became twisted and broke, too, thanks again to
glorious rust. Anyhow, I cut the flexible part of the pipe and
will replace these bits anew later on since everything is a bit
incurably rusty around here.
Efforts then shifted to the other side to try to remove the other
nipple but that too failed, so the caliper is removed, with a bit
less damage to the brake pipes, which seemed to be in better
condition on this side, but I must check for sure later. Both
calipers are now on their way to have their broken nipples
expertly drilled-out and thread re-tapped, hopefully.
Meanwhile efforts are made to replace the tie bar bushes and the
one on the driver's side is removed with a bit of general
wire-brushing to remove rust in the area, repainted and refitted.
After putting the new bushes back in place, the bolts on the rod
are torqued-up.
Meanwhile the expert engineer (Mac) who tries to repair my
calipers by removing the broken-off nipples sends the following
pictures showing the scale of the project at hand. Indeed the
broken-off nipples continued in their resolute refusal to budge so
with the prospect of heat- and acid-treatment being needed to
remove them, it became necessary to remove the seals and pistons.
A fair bit of gum was encountered in said process, although the
pistons cleaned-up very well in the end and a brush or spray of
paint has done absolute wonders. The awesomely expert and kind
engineer then decided to use another set of spare calipers since
my originals were a bit too far gone.
And here is how they look back on the car in early-mid December
2016.
Efforts are made to replace the passenger side tie bar bush but on
removing the bar, some quite bad cuts were found in the bar
itself.
Anyhow, a trip to the welder and all is repaired allowing the tie
bar and bush to be refitted.
A bit of a gap in events in mid-December 16 due to waiting for the
flexible brake pipe needed for the drivers side to arrive.
Around about Crimbo time in 2016 and the dodgy front brake pipes
(copper and flexible) are replaced on one side, the system bled,
tested and bled again and all seems to be awesome so it is given
another paint-up with a mixture of waxoyl and underseal.
So,
what's next in 2017?
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